The day was set as Saturday 20th
November 2010
The engine was completed as far as necessary
to allow a firing up to be tried.
The result was all a bit hit and
miss.
Several friends all gathered at 11:00
and established that fuel was being drawn into the carb so the ignition was
attached and on the first pull over it popped and smoked but nothing more
than one fire.
Then during the next 90 minutes everything
was tried and we had a second firing of about 5 ignition strokes and then
nothing.
After lunch one friend came back round
and we fitted the third piston ring with careful attention to width and depth
AND the fact the the rings have a top and a bottom which I did not realise
... was taken in to account and properly fitted. This gave much more compression
than when we left it before lunch.
Then on the first pull again engine did
run for 12 revolutions and the stopped and then another pull and it fired
and nearly got up to speed but finally petered to a stop.
That was a bit of luck as I then noticed
that the crank shaft has moved ... The Loctite 603 had let go ... So the
repair was made by reapplying 603 but the crank will need to come out and
I will be pinning it in all 4 places to stop that ever happening again
...
We also found at that too much fuel was
going into the engine ...
There is no disappointment on my part
for had it run without problems one would not have to work out why will it
not run and learn nothing ... Even motor engineer friend and all his experience
is at a loss as to why is does fire but then does not continue to
fire....
We have spark, fuel, compression but
that is it ...
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