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Small Parts 2

There are many small pasts to be made so this section is devoted to them
3rd November 2010

The cam I had water jet cut but then the profile to fit into the cam gear had to be machined. A fixing was created by using hex bar and machining to a good fit with a large nut with integral spacer.

Very small cuts were take of 0.3mm until the part reached near to the diameter for a press fit into the previously machined cam gear.

This photo shows the finished piece ready to press fit into the cam gear.
The cam press fitted (with Loctite 603) into the cam gear.

The cam gear is actually twice the width that it needs to be so changed to the supporting cam shaft will necessitate a re-make with a stepped bronze bush to fit into both pieces.

I think this is preferable to machining the gear thinner !!!

The modified cam bush in ph bronze. The bush originally designed was to support the whole of the cam and gear so to achieve this with the wider gear the bush was machined stepped to fit both pieces.

The bush has now been positions and secured with loctite 603. You can see that the bush is proud of the parts by 0.5mm to allow the bush to rub but not the parts on the adjacent elements.
The revised cam shaft to take the wider component of cam and gear.
The washer is now in place and nuts tightened down and the cam and gear are free to rotate with just the smallest amount of end float.
4th November 2010

The governor gear supplied did not have a hole bored through the centre.

As the gear had 17 teeth it was not possible to hold in a 4 jaw chuck and centre. I therefore turned the brass holder bored to the same external diameter of the gear and then a single saw cut was made to allow the brass to "spring". In fact is closed up so the gear had to be persuaded to enter.

As it had been bored the rear of the bore was flat to allow the gear to seat fully.

Now with the gear in the "collet" is was possible using the 4 jaw chuck and a DTI to centre, drill and ream 10mm.

The governor bush was a simple turning exercise starting at the lower end as in the picture and working towards to taper and then lastly the part was parted off.

It sits adjacent to the gear to show relative size.

The governor centre was to be a simple turning exercise but then i thought why not make it all in one piece and save having to silver solder items in place.

The part has yet to be tapped M3 and generally clean up to remove the machining marks and to adjust the profiles so that it has a pair of "ears" as the part that might have been silver soldered into place looks bottom right of the picture.

The governor shaft was another simple turning exercise with a 3.2mm hole drilled through the centre.
The governor shaft with its gear fitted by Loctite 603 as it just came out a mite too small but just right to Loctite.
5th November 2010

The governor wings have to have ball bearings silver soldered to them.

A slight depression was made in the soft heat resistant brick and a hole drilled to be a snug fit on the piece of 1/8" bar bent at right angle and used to hole everything in place whilst heating up and applying the silver solder.

The photo shows the "before" soldering.

After soldering a lot of clearing up was necessary as the surface of the ball and wing were blackened and aldo there was a residue of flux.

A special flux was used, obtained from the midlands Model Engineering show which came in powder form and was mixed to a paste with the consistency of single cream.

Here are all the parts of the governor. The centre "T" bar was machined from solid.  It is 3mm diameter and very gentle machining was necessary, and completed by filing of the "T" bar.

The "T" enables the wings of the governor to land nicely.

9th November 2010

The first of three oil pots has been made.

10th November 2010

The small push bar support bracket was machined from solid and a brass push bar spacer also made. These were then fitted to the timing plate. Note there is very little clearance between the gear and the piece.

12th November 2010

The brass end of the gudgeon pin were made.

13th November 2010

The key way has been cut in the gear. To achieve this a holder for the gear was machine as was done for the other gear.

This time the only material available to make the holder was steel so that was used and again a single saw cut enabled the holder to be held in the 3 jaw chuck and firmly grip the gear.

A key way and filed up the fit the gear.

A spacer was made up and a small notch filed so that it covered the keyway which was proud of the gear but lay flat to the gear.

TO BE CONTINUED